After couple of dozens good flights got unexpected crash into a pond. Was in Rate mode and did nothing in terms of throttle or pick/roll. Did not switch to RTH mode but think it hardly helped.
https://drive.google.com/file/d/1miXLvf2txF9bNK41G-43IVWP8fpEQ1Ri/view?usp=sharingThe quad was in water about 5 min. All props got broken - it make me think they were rotating right after diving. There were no more mechanical damages. I disconneted battery, and after couple of hours blowed the quad with hot air.
Switching on showed not working camera and video transmitter. But I've managed to fix them replacing some electronic parts. So the quad looks healthy now, not tried to fly though.
My setup:
FC - Revo mini with Next FW and IBus connection
ESC - DYS BL20A with BlHeli firmware
Motors - BG2204-2300kV
So the question is what's happened?
The most probable I guess is a ESC-motors interaction. On CC3D I used PWM/490, but after upgrade to Revo got some motor stuttering with sudden crashes. Switching to OneShot125 cured the problem but obviously not completely.
Will appreciate your ideas.