So after copious days with my transmitter issue, my librepilot pilot problem in Windows 10, learning to install Linux. Learning LibrePilot.
My build was completed. Test flight 1. And the yaw was out by 180deg. My quad was a great lawn mower.
Sitting here after Test flights 2,3,4. And Great news! It works. But bad news I crashed. Lots of adjustment to do.
Main issue is I set calibration as not to recalibrate on arming meaning that once in the field it got a knock. I had no way I know of resetting the gyro.
I should then, have gone home.
But No.
I had two setups mapped to F-mode one was far to gentle to compensate against the breeze. And the other, well great fun but let's just wait until I'm a bit more experienced for this setup!
Anyway back to do some setting up. And repairs and Calibration.
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