i have a dys 250 quad, cc3d board and has been running fine for about 2 months. i found that the motors would stop spinning at the lowest throttle value so i played around with the motor outputs section for a while and it totally screwed up the way my quad flys. when i apply throttle, one motor (the same one consistently) on the quad always banks downwards without me commanding it to, the more the throttle the more it banks. when taking of the quad wants to bank to the right a large amount. when switching flight modes the quad also corrects itself to the same right banked position as if it thinks its level even though the gyros have been calibrated multiple times. any help would be appreciated with this as i was enjoying my quad so much and its my first so i don't have much experience with trouble shooting.