Today I noticed that Analog Airspeed Sensor functionality is broken in current next. Revo board, MPXV7002 sensor on output port #5 (ADCRouting: [adc4]). No errors or alarms but sensor values are nonsense and do not reflect the output voltage from the sensor. Disconnecting the sensor doesnot affect displayed raw values, too.
The sensor and Revo board are ok, I switched back to 16.09 to confirm they are functional.
Can someone test and confirm this issue?
Here is the UAV file for the wing, for firmware next.589: