LibrePilot Forum
General Category => General Discussion => Topic started by: utoedter on March 07, 2017, 02:34:42 pm
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Hello all,
Ive changed the FC from my Eachine Racer from the genuine CC3D which was installed by default to a Mini Revolution Board. I did all the calibration stuff, used the same output settings (490Hz) but if i fly in complementary mode, the quad twitches. Its not serious , you can control the quad without problems, but its visible and hearable. With the normal CC3D board the quad flies very stable. Increasing the gyro noise filtering to a very high value of 0.4 reduced the problem, but it still exists. Any hints are welcome.
Udo
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Problem solved, other as stated. one output channel used 50Hz update rate, the 3 others 490Hz. Sometimes im blind. 8)
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you are lucky (probably "smart" is a very term) because I can't even get my Revolution board/Eachine250 Racer to work. I cant seem to get the mag and gps calibration to work. Any tips? Thanks.