LibrePilot Forum
Development => GCS General => Topic started by: jtrout19 on November 06, 2016, 09:27:53 am
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Hey geys I have been trying to solve an issue all night and need some help. On a side note I finally got my mag working by building this https://www.rcgroups.com/forums/showpost.php?p=30987654&postcount=296https://www.rcgroups.com/forums/showpost.php?p=30987654&postcount=296 (https://www.rcgroups.com/forums/showpost.php?p=30987654&postcount=296https://www.rcgroups.com/forums/showpost.php?p=30987654&postcount=296) Works Great!
Anyone the little window with the picture of a quad that moves with your quad in the bottom left corner of the flight data tab, well its showing my quad pitched at like ~45 degree angle. The atrtificial horizon line shows perfectly level. What is going on with this?
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This occurs if you shifted/rotated the view using a mouse.
You can simply resolve this issue restarting the Gcs or reset the view:
- click the modelview to give focus,
- hit the space bar in your keyboard.
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Lord that was too easy.... thank you......very much
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...I finally got my mag working by building this https://www.rcgroups.com/forums/showpost.php?p=30987654&postcount=296https://www.rcgroups.com/forums/showpost.php?p=30987654&postcount=296 (https://www.rcgroups.com/forums/showpost.php?p=30987654&postcount=296https://www.rcgroups.com/forums/showpost.php?p=30987654&postcount=296) Works Great! ...
That adapter by pawelsky is what the Chinese copied to make the DJI Naza clone GPS units. They actually run his firmware unmodified.
It's a good solution for people who already own a two connector gps/mag and need to free up one of the ports for something else like an OSD.
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Yip thats what I got going on too, plus i read somewhere that Mag over I2C has issues. I am using S.BUS and my RX does not support PPM (FrSKY X6R) so that is why I ended up building this. I also purchased a SBUS to CPPM converter but got tired of waiting on it to arrive in the mail.
I also used autotune last night as well. The quad flies amazing for as much as I could fly it at night in the rural area I am in. Will fly today more to see if PIDs are good. I will say that the PIDs autotune got are way different from what I got. I finally found a use for my arduino's though. I have 5 minis and 8 unos. I have a mix of the large DIP atmega uno and the SMD version which has the same ATMEGA that is on the Micro Minimosd.
I wish i could learn to program like a JEDI. Would love to help you guys develop things. Specifically I would love to come up with a Color OSD. Maybe one day......
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I would be interested to know now the one tune works compared to the other.
Two main things to test:
- fast forward flight in Attitude mode holding a significant amount of forward stick. Suddenly release the forward stick to where you are only holding a small amount of forward stick. Does it "pop up" as if you gave it a lot of back stick?
- descending straight down, no wind, at slow to medium speed. Does one hold attitude better than the other and not wobble all over the place?
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Well i unhooked it last night due to the issues i have been having with gps and mag calibration. But may be hooking it back up because i cannot get the flight controller to recognize the gps now. Went back and set everything to ublox and mag works over i2c but no gps. I have 2 naza clones coming in the mail. But wont be here for about a week. I still need to make video of everything and i may document everything i do this time around with arduino unit to make sure there are no issues.